Well, it has just been a waiting game. I plastigauged the motor with the new bearings I bought and found that I needed oversized bearings for my main bearings. So after another week I was able to button the motor up.
After putting the motor in the car, I realized I needed an oil filter relocation kit. The oil filter won't clear the 3" dp. So I went out and found someone locally selling a kit for his sons 5sfte setup.
Heres a pic of the motor assembled minus the oil filter relocation kit.

Since then I have put the motor in the car and have her running. I am idling a bit high, thinking it maybe the isc resistor in the ecu.
It could be a vacuum leak though, since the gasket kit came with 2 throttle body gaskets for some reason.
Or it could be the notching I did on my intake manifold to throttle body for the ISC. I didn't make it big enough. If that were the case, I can live with a 1000 rpm idle.
I'll take more pics of the motor in the bay.
Oh so far I have 2 miles on her. and btw the valve cover is super scuffed up now after having to pull the motor 2 more times after original install due to some issues with the transmission.
And cams not lined up properly, stupid 3sge cams. They don't have a notch to line up with the cam cap near the cam gear.